I finally finished my 1977 DS II centerboard saga yesterday. Thanks to this forum, I saved myself a lot of time, aggravatiion and expense.
I started down this road because the centerboard would not go all the way down no matter how hard we tugged on the lowering rig. So I read all the form entries about
centerboards and got started. For once in my life I looked before I leaped. My wife was amazed.
My name is Rowe, pronounced row, so it seemed natural to name the boat "The Rowe Boat." Especially since I have a fondness for puns.
So I trailered The Rowe Boat into the back yard and tied a yoke around the stern cleats. This I attached to a handy tree and then gently pulled the trailer out from under
the old girl. Using the crowbar-tiedown method (thanks, forum attendees) I careened her over until the mast was pretty much horizontal. Now, I tried the method someone
outlined of constructing a sawhorse type brace to cradle the bow, and that worked for a while. But the lines I was using to keep the bow up high enough to get her back on
the trailer eventually slipped off. Bummer, that.
From there I was able to get the pivot bolt out by contorting myself a lot. I unrigged the board and pulled it out to see what was up. It was pretty scuzzy all around.
A previous owner had made some repairs to the centeroard trunk/hull joint with some kind of auto body filler putty without sanding any of it down. He or she obviously had
done this without removing the centerboard because the lousy repairs made it tough to get the board all the way out. And tough to get all the way down in the water! When I
did get the board free, I saw that someone had drilled a neat hole in it about 3/4 of the way to the aft or lower end, obviously to let water in. Itg was still wet. Perhaps
that someone thought the board was too light. But the hole was about 1/4 inch across, so it would take a while to fill the hollows of the centerboard with water.
After cleaning the scuzz off the board and sanding it smooth, I considered what to do next. Since I don't have any intention of racing The Rowe Boat, so I wasn't worried
about the board's weight--except for letting it down gracefully and bringing it back up. So I usd a hole saw to cut out a 1-1/4 inch plug over the existing small hole and
filled that hollow with number 8 lead shot set in unthickened epoxy. I added about eight pounds of lead to bring the board's weight up to about 29 pounds. Should I ever
decide to get back within class limits, I might buy a new centerboard.
Then I patched my hole with its cutout and some 'glass tape set in thickened epoxy. I also filled some deep scratches and a couple of significant dings. Finally, I sanded it
again and blessed it with a rolled and tipped coat of unthickened epoxy. I had thought about covering it with some light fiberglass, but I didn't want to increase its width
much at all.
Now, time to do something about all that body filler in the hull! I scraped it out not only from around the centerboard trunk, but from the keel forward as well. I couldn't
see anything that looked like cracks, but I decided not to take a chance. So I reinforced the centerboard trunk's joint at the hull and the keel forward up to the waterline
with 3-inch tape set in thickened epoxy. It doesn't look so wonderful as-is, but gel-coat should hide these sins. Right now, it's time to get into the water.
Yesterday, I got the centerboard back into the hull and bolted without help. With the boat careened, the board did not try to fall out, so no one was needed to struggle
under the boat to position the board and hold it just so. I marked the location of the pivot from the outside/lower edge of the board with a try-square and a marker, set a
white piece of dowel in the pivot hole so it rested through the (careened) upper side of the trunk on the centerboard itself, then used a powerful flashlight to see where
things were. I only had to move the board a bit of an inch this way or that, several times, before the dowel fell through.
Right, I should have put something on it to keep it from doing that. Oh, well, I'll see if I can hear it rattling around when I tack.
Much to my surprise, the pivot bolt went right through. So I bedded both washers and began the lengthy process of tightening the bolt. That was frustrating, so I made
absolutely sure the nut was on well enough not to fall off at any time during any jostling and decided to finish tightening it when everything was upright on the trailer.
Getting the boat back on a non-tilting, rather inexpensive trailer alone was an exercise in levers and fulcrums, winches and lubricants. But I managed.
My wife isn't thrilled about the trampled grass (read: pretty dead, really) in the back yard, but I think I will try to design something a little more permanent and
hull-friendly. Like a couple of 4x4's 12 feet long covered on their upper surfaces with carpeting and set in a sturdy, steadying frame. I have a scissors jack I could
stabilize and use to lift the front of such a rig up to trailer bunk height when all my under-hull work was done. Careening would be simple and the careened hull would rest
on supports that would keep the "rub rails" off the ground.
We shall see.
Thank you, forum denizens! This is a great place for information and I hope I have offered some help and hope as well.
Bob Rowe (rowerw-at-comcast.net)